Composite Plugging Removal Technology and Application in Low Permeability Oilfield
In an oilfield factory, the blocking and jam in Chang 2 reservoir is very serious. In recentyears, according to analysizing different plugging mechanism and optimizing acidizing formula, theoptimal plugging removal technology was formed suitable for the solution for the Chang 2 reservoirof oilfield...
Gespeichert in:
Veröffentlicht in: | Diffusion and defect data. Solid state data. Pt. A, Defect and diffusion forum Defect and diffusion forum, 2019-08, Vol.394, p.9-13 |
---|---|
Hauptverfasser: | , , , , , , |
Format: | Artikel |
Sprache: | eng |
Schlagworte: | |
Online-Zugang: | Volltext |
Tags: |
Tag hinzufügen
Keine Tags, Fügen Sie den ersten Tag hinzu!
|
Zusammenfassung: | In an oilfield factory, the blocking and jam in Chang 2 reservoir is very serious. In recentyears, according to analysizing different plugging mechanism and optimizing acidizing formula, theoptimal plugging removal technology was formed suitable for the solution for the Chang 2 reservoirof oilfield factory. This plugging removal formula increases the efficiency radius, and increases thedosage of additives to protect the pipe, rod and pump from the precipitation such as Ca2+and Mg2+,which causes new pollution. Reasonable multiple technologies were designed, and low displacementmethod was used in the injection process, aiming at the characteristics of Chang 2 reservoir. Thismethod extends the time of plugging removal fluid staying around the well bore, which can eliminateplugging near well bore area effectively, and improve the permeability. DQ-1 composite pluggingremoval and other kinds of plugging removal methods have been used more than 50 times, and theeffect is remarkable, which made a positive contribution to stable production of the oilfield. |
---|---|
ISSN: | 1012-0386 1662-9507 1662-9507 |
DOI: | 10.4028/www.scientific.net/DDF.394.9 |