降低抽油井检泵率和综合返工率的措施
分析了抽油机井检泵率上升的原因,并采取了串联式凡尔罩、油管柱锚定、接箍扶正器和防砂技术等措施,治理偏磨井,降低了油井检泵率和综合返工率,可延长检泵周期。应用表明,推广四项技术措施后,检泵率年度同期对比下降2.4个百分点,综合返工率年度同期对比下降0.8个百分点,抽油机井检泵综合返工率由去年同期的16.2%下降到15.4%,治理效果显著。...
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description | 分析了抽油机井检泵率上升的原因,并采取了串联式凡尔罩、油管柱锚定、接箍扶正器和防砂技术等措施,治理偏磨井,降低了油井检泵率和综合返工率,可延长检泵周期。应用表明,推广四项技术措施后,检泵率年度同期对比下降2.4个百分点,综合返工率年度同期对比下降0.8个百分点,抽油机井检泵综合返工率由去年同期的16.2%下降到15.4%,治理效果显著。 |
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subjects | 偏磨井 实用技术 治理 |
title | 降低抽油井检泵率和综合返工率的措施 |
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